Around christmas I did order some parts and last week most of them dropped in.
Most important the fan and today was the day to change the old with the new.
After a cup of coffee I did lay out the wiring, since that is the part I'm having the most problems with this helps me a lot:
Then a picture of a battery clamp I couldn't use.
The Terrano has an extra wire clamped and this one can't do the trick. Will be ordering the right one soon.
Then it was time to go to the shed where I did park the truck the evening before. Removed the radiator and the old fan and the front part of the viscous coupling.
The second part is compressed to the belt bearing so couldn't remove that one.
After this I test fitted my new fan, but it was just 2 mm's to thick to fit in the space I had planned :doh
So it was time for plan B. But...just one more picture of the old vs the new one:
Right, new fan in place:
After the first plan failed I moved it a bit to the side, orriginaly I wanted it to be in the center so the old shroud would fit like a glove.
Now my plan is to make it fit again.
When everything was fitted back and it was time for the wiring.
No pictures since my focus was to big :lol
The Monster Cooling fan has an option to place a switch in between as well as an override, so to check my work I made a small bit of wiring to check if everything would work okay and luckily it did!
Removed the switch again and put everything nice into it's place.
Also my plan was to fit a thermostat I could put on the desired temperature, but again plan B since it hasn't arrived yet and there was a fixed one with the fan.
Goes on at 82 degrees Celsius so that is fine as well.
After installing the thermostat I filled everything back up again and started to change the inlet hose of the turbo.
Takes no time to change, but finding a new one for a decent price does...
This was the old one, the new one hasn't got a crack in the place where the tape is on this one :naughty
After this I did a quick testrun in the back yard and was releived the noise was gone and the engine did respond like it used to, or even a little bit better
Got a lunch and afterwards I did 20 miles of testing and had to bleed the coolingsystem twice, but finally result:
Needle right in the middle and it didn't came of it again.
My testing included:
- city traffic
- highway speeding and more
- 4x4
- slow driving with a lot of stops and a heavy trailer behind the truck
After testing the fan kicked in for about 5 seconds when I killed the engine so that is perfect!
For now I am a happy man again